We finally had a enough bad weather in a row for me to look deeper. To cut to the chase - the problem is solved.
I found 14 of the 16 valves too tight with a capital OH MY. number one intake were both just fine. I adjusted the vavles, removed all non factory wiring, new oil and filter, cleaned and gapped plugs ensured good fuel flow and good grief! It's like a new bike. Just got back from 106 mile shake down trip and I could not be happier! No more stalling, lots of power and speed - in short, it's everything I'd hope it would be.
While it was all apart I added LED dash and clock lights and just look over everything. replaced bunch of the tupperware bolts with hex heads with washers (which is what I had in the house, not because it looks the best

)
I wonder if the resistor mod to the fuel gauge could get added to the back of the dash panel at the gauge? I didn't have the right resistor in the house, so that will be another project for later.
Now, I really need to find a good( not terribly exPensive) seat because this one on there stinks

Thanks to all you people that took the time to post how to's and write ups on things. What a treasure trove of knowledge to tap into.

Y'all get a cold drink and pretend I bought it for ya!
Thanks,

Peter